Question: Q 1 . A batch settling test has been performed on an industrial wastewater having an initial suspended solid of 5 9 7 m g

Q1. A batch settling test has been performed on an industrial wastewater having an initial suspended solid of
597mgI to develop criteria for the design of a primary clarifier. The test column was 5in. in diameter and 8ft high,
and sampling ports were located 2,4,6, and 8ft from the water surface in the column. The suspended solids
remaining after various sampling times are given in table below. The wastewater flow is 2.5MGD. Determine:
a. The design overflow rate and detention time if 65% of the suspended solids are to be removed. Use scale-
up factors of 0.65 for the overflow and 1.75 for the detention time.
b. The diameter if a circular clarifier is used
c. The design diameter of the clarifier if equipment is available in 5-ft increments
d. The depth of the tank
Depth, ft Time, min
1020304560
2394352243182148
4460406337295216
6512429376318306
810181142120813151405
Q 1 . A batch settling test has been performed on

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