Question: Statistical Process Control at Motorola: Traditional quality control methods identify variation as the enemy of ensuring quality. However, the control of variation by itself can
Statistical Process Control at Motorola: Traditional quality control methods identify
variation as the enemy of ensuring quality. However, the control of variation by itself can
never achieve the remarkably low nonconformance rates of world-class quality leaders.
The best methods for controlling variation, mistakes and complexity are each forms of
mistake proofing. Using these mistake-proofing techniques, virtually every mistake and
non-conformance can be controlled at a fraction of the cost of traditional quality control
methods.
The FZU-48 fuze initiator (for the FMU-l39 bomb fuze) programme in the Tactical
Electronics Division (TED) of Motorola moved quickly and smoothly from the design
stage to the full-scale high-volume production stage by utilizing statistical process control
(spc) techniques. Virtually all phases of product manufacturing (design, assembly, tooling,
machines, test equipment and inspection) used SPC and problem-solving techniques (PST).
The result was a system capable of delivering excellent product quality and achieving a
high volume production output.
All machinery, tooling and fixtures were carefully designed with a zero defect approach.
A team of engineers trained in SPC carefully reviewed the design prints in a brainstorming/
failure analysis and correction mode to minimize design flaws during production. After the
machines, test equipment, tools and other peripherals arrived, they underwent carefully
planned machine capability studies.
The machine capability studies comprised two phases. First, a capability index (Cpk) and
a capability potential (Cp) were calculated for all critical variables followed by tests for
statistical control. Next, reduction of variation was performed when the capability index
failed to meet the planned target Cpk index of greater than 1.0 (factored by a four sigma
spread). During the reduction of variation, variables contributing to variation were
identified and either removed or reduced to a controllable level. The capability studies
helped to predict the performance of the equipment with a level of certainty and to
collectively determine whether the process had sufficiently low variability to meet process
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specifications. It also served to uncover areas of potential problems before production and
encouraged efforts to prevent production of non-conformance products. Seventy per cent
of the machines (test equipment, tools, etc.) had a capability index Cpk higher than 2.0
(planned goal Cpk) and the other 30 per cent exceeded a Cpk of 1.0. The Final Lanyard
Pin Press experienced seven cycles of machine capability studies and redesign before it
was considered unsuitable for production and replaced by a new machine.
During the various stages of production, many problems arose and were aggressively
corrected utilizing PST and SPC techniques. PST techniques included brainstorming
sessions, cause-and-effect diagrams and Pareto diagrams. SPC techniques included
variable search and statistically designed single-factor and full factorial experiments.
Ishikawa (cause-and-effect) diagrams, design of experiments (DOE) and brainstorming
were used to solve complex problems such as the epoxy leakage through the end cap towers
reducing the defective rate from 68 per cent to less than 0.1 per cent. The use of DOE was
also effective in correcting the problem of high shearing force for lanyard separation, which
failed to shear at a force of 148 + 20 lbs-f. A two by three (three factors, two levels) full
factorial experiment was designed and conducted yielding accountability for 96 per cent of
the variation. The standard deviation of the shearing force prior to experimentation was 34
and was successfully reduced to 3.3. After the completion of the first 115 deliverable FZU-
48 units, an unforeseen design flaw resulted in the failure of the First Article Acceptance
Test. Aggressive utilization of PST and DOE techniques by a team comprising design,
manufacturing, quality assurance and test engineers corrected the problem. In a period of
five weeks, 14 consecutive statistically designed experiments were conducted, leading to
product design changes and reduction of product performance variability. The standard
deviation of the cover opening force of the unit prior to experimentation was 34.58. It was
reduced to 4.70, thereby achieving a Cpk equal to 2.20 and exceeding Motorola's Six
Sigma design objective (see Table: 1).
Table: 1 FZU-48 Bomb Fuze InitiatorOpening Force
Specification
Distribution No. 1:
Average: 101.63, Standard Deviation: 34.58
Cp = 0.34 , Cpk = 0.00, PPM = 539130
LSL: 30
Nominal: 65
USL: 100
Distribution No. 2
Average: 60.7 , Standard Deviation: 4.7
Cp = 2.48 , Cpk = 2.18, PPM = 5.199E 05
Since production began in early August 1987, the FZU-48 programme has increased its
production by ten times, from 50 units per day initially to 550 units per day. During this
period, eight consecutive lot acceptance tests (LATs) have been conducted and passed. Of
all the units tested during the LATs, one unit failed. That unit was later found to have a
piece part out of tolerance that caused the failure. The team of SPC experts responsible for
applying the SPC techniques consisted of Adi K. Bhote, TED SPC coordinator for the
Manufacturing Board Assembly Area; Jim Blanden, TED Manufacturing SPC specialist;
and Mario Perez-Wilson, Divisional SPC manager, Small Signal & Sensor Products
Division, Semiconductor Products Sector, and former SPC coordinator for the FZU-48 and
FMU-139 programmes.
Contributing their engineering expertise and support were Jim Gardner, senior test
equipment engineer, Ron Meyer, lead design engineer, and Pete Rendek, lead design
engineer. Management commitment and support to implement SPC from the design stages
was provided by Kevin Mulroy, then a quality assurance team member and Ray Beliveau,
manufacturing team member. "The FZU-48 programme is probably the first programme in
Motorola that utilized SPC techniques from the very beginning. This programme has been
quoted by the customer as being their first programme to go from design to full-scale
production in a fast and smooth manner. The major ingredient for this success has been the
implementation of SPC," Mario said. No blueprint exists for the successful implementation
of SPC in a production system. However, the SPC techniques used on the FZU-48
programmed can facilitate a smooth transition from design to full-scale production on other
programmes if they are performed as early as possible prior to production. On the FZU-48
programme, potential problems were detected using machine/process capability studies,
statistically quantified using descriptive statistics and probabilities and statistically
corrected with statistically designed experiments. After implementation, the corrections
were statistically validated. The end result was a high-quality output.
Instructions
i. Why was statistical process control (SPC) introduced in the FZO-48 fuze initiator
programme?
ii. How did process capability studies help the division?
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