Question: A batch settling test has been performed on an industrial wastewater having an initial suspended solids of 5 9 7 mg / L to develop

A batch settling test has been performed on an industrial wastewater having an initial
suspended solids of 597 mg/L to develop criteria for the design of a primary clarifier. The test
column was 5 in. in diameter and 8 ft high, and sampling ports were located 2,4,6, and 8 ft from
the water surface in the column. The suspended solids remaining after the various sampling
times are given below:
The wastewater flow is 2.5 MGD.
Determine:
a. The design overflow rate and detention time if 65% percent of the suspended solids are to
be removed. Use scale-up factors: 0.65 for overflow rate and 1.75 for detention time.
b. The diameter if a circular clarifier is used.
c. The design diameter if equipment is available in 5-ft increments of tank diameter.
d. The depth of the tank.
Time (min)
Depth, ft 1020304560
2394352243182148
4460406337295216
6512429376318306
810181142120813151405

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